By Tommy H. Thomason
Saturday, August 23, 2008
Single-Seat A-6
The Navy's VA(L) was to be a single-seat, single-engine attack airplane with an overload mission of 12 Mk 82 (500-lb) Snakeye bombs delivered at a radius of 600 nautical miles. Another key requirement was that it be "a modification of an airplane currently in the Navy inventory." The payload/range favored the use of the Navy's new TF30 engine.
Grumman considered proposing either a TF30-powered F11F or a single-seat modification of its A-6 Intruder with a single seat but the existing engines. The latter's size enabled it to easily exceed the payload/range requirement even though it did not have the fuel-efficient turbofan engine. (Although the A-6's size was a drawback from the spot factor standpoint, it could be mitigated by folding the horizontal tail; see http://thanlont.blogspot.com/2009/06/minimizing-spot-factor.html.) Grumman decided to offer the A-6 derivative believing that the low development cost and commonality with an existing airplane in the air group would trump the somewhat higher unit cost.
It didn't.
Douglas proposed a supersized version of its A4D.
North American did the same with its FJ-4.
Vought won the VA(L) competition with an F8U Crusader derivative with an even more creative interpretation of the "modification" requirement than Douglas or North American proposed.
For a last minute change in the Vought proposal, see http://thanlont.blogspot.com/2009/06/it-takes-all-running-you-can-do-to-stay.html
Sunday, August 17, 2008
Attack Crusader

Thanks to the Vought Aircraft Heritage Foundation for the photo.
Saturday, August 2, 2008
Little known (and unsuccessful) Proposals

My guess is that it was an attempt to take advantage of the A2D troubles at the time. Douglas got a letter of intent for the T40 turboprop-engine-powered A2D in June 1947. It was supposed to fly in March 1949. Because of T40 engine problems, it didn't fly until May 1950.
Thanks to the Glenn L. Martin Maryland Aviation Museum for the illustration.
Thursday, July 24, 2008
Still not easy

The WWII problem - hit an aircraft carrier steaming at 33 knots with a torpedo that runs at 33 knots. This example is a drop roughly abeam the 800-ft long carrier at 2,000 feet, well inside the 1,000 yards usually cited as the maximum drop distance for accuracy. I've revised the calculation to roughly account for a drop from 200 feet (3.5 seconds of air time) and 200 knots, which increases the average speed of the torpedo significantly and therefore reduces the lead required. It's now obvious that the lead is sensitive to the drop speed and altitude, the ballistics (lift/drag) of the torpedo in the air, and the deceleration of the torpedo in the water until it is at its run speed of 33 knots. The good news is that the lead determination is less sensitive to the target speed, although it's still important, and the ship has less time to turn into or away from the torpedo track.
Thursday, July 17, 2008
Sticking With What You Know


Pictures and information courtesy of the Glenn L. Martin Maryland Aviation Museum.
Thursday, July 10, 2008
This Just Isn't Right

The production airplane was originally the WF-2, redesignated in 1962 as the E-1B. Strictly speaking, there was a WF-1 but not an E-1A, since the WF-1 was cancelled at the mockup stage. It was to be an S2F airframe simply modified with an APS-20A mounted above the cockpit. This would have preserved the original empennage and wing fold arrangement, albeit with the addition of small fins on the horizontal stabilizer to maintain directional stability.
Friday, July 4, 2008
XFL-1 Carrier Suitability Evaluation

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